FK70煤层气井井壁失稳钻具卡埋成因分析及治理

Cause Analysis and Governance of Well Wall Instability and Drilling Tool Jamming in FK70 Coalbed Methane Well

  • 摘要: 在阜康白杨矿区1号煤层气FK70井钻进至八道湾组上段(J1b3)黑色炭质泥岩段时,发生了三次井壁失稳和钻具卡埋,通过分析地层失稳机理,发现影响因素包括高黏土矿物含量、大倾角地层、微裂缝发育及欠压实等。第三次侧钻施工中,首次采用以成膜封堵剂多元乙烯基高分子乳液FDM-1为主的化学成膜封堵防塌技术,并结合纳米级及亚微米级封堵剂,优化了钻井液体系的封堵防塌性能,成功钻穿垮塌层段。

     

    Abstract: When drilling into the black carbonaceous mudstone section of the upper part of Badaowan Formation (J1b3) in the No.1 coalbed methane FK70 well in Baiyang mining area of Fukang, three times of well wall instability and drilling tool jamming occurred. Through analyzing the mechanism of strata instability, it is found that the influencing factors include high clay mineral content, large dip angle strata, micro crack development, and undercompaction, etc. During the third time of side drilling construction, the chemical film-forming sealing and anti-collapse technology, mainly based on the film-forming sealing agent, polyvinyl high polymer emulsion FDM-1, is adopted for the first time, the sealing and anti-collapse performance of the well drilling fluid system is optimized by combining the nanoscale and sub-micron level sealing agents, and the collapsed section is successfully drilled through.

     

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